Making progress now! Today I worked a couple more of the squawks we need to have fixed before we can reinstall the tail section. I found out what was happening with one of the vertical stabilizer mount bolts. When I inspected them one of them looked funny around the nut. Today I pulled the bolt and found a washer that was meant for a shouldered bolt to be there and a little squashed and oblong. Easy fix by replacing the washer and torqueing the bolt. Here's the washer I removed on the right in this picture.
I put the airplane in the air on jacks in preparation to reshim the left hand downlock. There is a little too much play in the gear sideload when in the lock, so I'm going to try to shim it into spec. It should be between .001-.007 and I'm a little over that. Here's a picture of the downlock and the stop. The shims go under the stop.
I also pulled out the emergency motor and pump and got my bath of hydraulic fluid. Never fails that I wear it if I mess with it. Tom reinstalled the new motor and pump. I warned him about the dose of 5606 he might get. I'll have to ask if he had better luck than I did. Here's 2 pictures of the motor and pump removed and new ones installed.
This past weekend I primed the new nose gear that we'll be installing soon. We'll get the tail section done and tackle this probably on Sunday. Here's the parts ready for paint. I plan to paint them tomorrow night if able.
David
WHF Maint