Hi Everyone & thanks for all the replies, some excellent information and viewpoints - all very much appreciated + some fascinating "bonus" information as well!
A bit more on the crash - there are two reports that form parts of the original 1945 Investigation report. The first states that:
The Mustang was seen to make a shallow dive from about 1,000ft over the village and then climb up again and commence another dive, this time from about 800 ft, again on a south-north heading having orbited the village. It was then seen to complete a roll to the left, steady momentarily, and then begin another roll to the left. During the second roll the pilot was seen to leave the aircraft, which immediately dived vertically to the ground with the engine running.
The second differs slightly:
The witnesses statements indicate that he made a shallow dive at about 1000 feet over the village and then climbed up to approximately 700 to 800 feet, and then commenced to orbit the village. Again on a South to North heading he commenced another dive immediately rolled over to the left again still losing height. During this roll the pilot was seen to leave the aircraft and the aircraft completed a roll and immediately dived straight into the ground at high speed. The pilot was thrown forward and was found 40 yards ahead of the crash with his parachute open but undeveloped and parachute cords around his legs.
The aircraft was new having been assembled at Lockheeds at Renfrew after being shipped over to the UK. Comments were made about the difficulty in adjusting the harness straps and that the pilot followed the common British ferry pilot practice of sitting on the aircraft's manuals and logbooks - I would think this lot would create a veritable snowstorm of paperwork if flown with the canopy open?
Comments are made elsewhere in the report about observed injuries including possible bruising to the eyelids and "suffusion" of the eyes, which it was thought might indicate the effects of negative G - though medical opinion seems to have been divided and it also says a severe blow to the head could have caused this - in view of what happened to the unfortunate chap and an eyewitness I have spoken to, who described the impression he left in the field where he came down, makes me wonder how any of his injuries could be attributed so specifically!
I really am not happy with the report, as it lays the blame on the pilot for carrying out unauthorised aerobatics and makes comments about his psychological state. The manoeuvres made were hardly spectacular aerobatics and even the report concedes that there was really no one around to see them anyway. The more I looked at the details, the more it reminds me of another incident we investigated a couple of years ago - P-51B Mustang 43-6635
http://www.south-lancs-aviation.co.uk/N ... 3-6635.htm also lost on a routine ferry flight. That aircraft was newly assembled at Speke and was being flown to Warton for further modification, when it suffered a fuel or glycol leak - the pilot, Flight Officer Eugene Stanley Rybaczek, tried to save the aircraft and to put it down on a satellite landing ground at Knowsley Park. Witnesses saw vapour streaming from the obviously open cockpit and the aircraft made unexpected manoeuvres before it stalled and crashed on the threshold of the runway.
Could this chap have opened the canopy to try to clear such a problem and then lost control? Others have said the manoeuvres appear more like he was testing the aircraft or had a control problem?
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Regards - Nick - Lancashire UK
"Ex tenebris Lux"
http://laituk.org/